JOURNAL OF YANGTZE RIVER SCIENTIFIC RESEARCH INSTI ›› 2019, Vol. 36 ›› Issue (10): 180-184.DOI: 10.11988/ckyyb.20190863

• TREATMENT OF DYKE RISKS • Previous Articles    

Effectiveness of Vertical Anti-seepage Body in Typical Levee Segment ofHuaihe River Drainage Project: Analysis and Evaluation

FENG Di1, WANG Yuan1, GAO Shan2, YU Chang-wei1   

  1. 1.College of Civil and Transportation Engineering, Hohai University, Nanjing 210098, China;
    2.Authority of Regulation Project of Diverting Huaihe River into Xinyi River, Yangzhou 225002, China
  • Received:2019-07-22 Online:2019-10-01 Published:2019-10-21

Abstract: Despite wide application of vertical anti-seepage reinforcement in embankments, the effectiveness of anti-seepage is difficult to be detected and evaluated after the anti-seepage project is finished due to the complexity of geological conditions and concealment of project. In this paper we analyzed the effects of vertical anti-seepage body, the depth, damage location, and integrity of anti-seepage body on the seepage field of levee by numerical simulation taking the regulation project of diverting Huaihe River into Xinyi River as a case study. We further examined the effectiveness of anti-seepage body by comparing the hydraulic gradient of spill point with the allowable hydraulic gradient of soil. Results show that the head behind the anti-seepage body decreased markedly after the vertical seepage control treatment was carried out on the levee. The bottom of anti-seepage body inserting into the clay layer of levee had better impervious effect than that of anti-seepage body not inserting into clay layer. In the presence of defectives, the infiltration line rose obviously behind the anti-seepage body. The hydraulic gradient in all conditions at the spill point was smaller than the allowable hydraulic gradient, indicating evident seepage control effect.

Key words: levee project, vertical anti-seepage body, seepage field, effectiveness of seepage-control, evaluation

CLC Number: 

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